Work Session

November 14, 2020

 

To join the fun, contact the railroad at: WorkSession @ RedRiverAndGulf.net (no spaces)

 

Team:
Mike
Glen

Wimbley

Doug (SFHM Staff)
Domineaux (RRG staff)

Tucker

Everett

Jason

 

Summary:
The right people with a good plan and quality expertise and tools made for great work on a beautiful fall weekend. Thank you to all for volunteering!

 

Accomplishments:

Accomplishments:
- Flat/ punctured/ junk car tires and equipment tires brought to disposal pile
- Switch tie at Switch #7 / Switchback Jct stabilized with blocking
- Free log car trucks and water tank car frame pushed to end of siding (to free up storage track space and allow for more vegetation spraying)
- Gallery (bench) car and derrick (crane) brought into engine house and placed over pit for inspection and repair
- Main Line Switch / Switch #8 (immediately by McGiffert) leveled and repaired to safe operating order
- Light fixtures and small horsepower motors relocated from engine house to newer powerhouse at sawmill
- Locomotive 202's air compressor relocated to machine shop and placed behind 202
- Tool room organized and cleaned up
- General Engine House re-organization and cleanup (empty out garbage cans, round up scrap / junk metal to scrap bin, relocate parts

   and equipment to appropriate long-term storage)

 

 

Friday
Before the Board of Directors meeting, I used the tractor and chains to dispose of the pile of old, flat, punctured, and junk tires pulled out of the Engine House as part of an earlier cleanup. After the Board meeting, Everett cut some lumber to block up Switch #7 / Switchback Junction switch to prevent twisting on the switch tie and the switch stand. Mike, Doug, and I used the tractor and chains to push the log car trucks to the end of the storage siding. We hit a metal bar we couldn't see in the vines and the first truck derailed. After much jacking and blocking, the truck was re-railed, the bar removed, and the trucks rolled freely. Next, we pulled out the water tank car frame sans water tank out past the switch and the road crossing. We chained it to prevent it from rolling, then we pulled out the gallery (bench) car and connected it to M2 to tote back to the Engine House pit for inspection and repair. Due to a cross level and track gauge issue, the M2 front axle derailed en route to the engine house at switch #8. Tractor and chains re-railed the M2. The water tank car frame was pulled back to the end of the storage siding once the crane and bench car were relocated to the Engine House.


Saturday - Morning
Mike, Glen, Wimbley, Everett, Jason and I tackled the cross level and gauge issue at Switch #8. The expertise of all involved, along with plenty of hands, had this project finished within the morning. Track jacks and wood blocks cut from scrap lumber on hand were used to level off the ties. Mike operated the heating torch while Glen and Wimbley used a claw bar and a lining bar to put a proper bend in the switch rod (as the switch points were high and the bolts were preventing proper closure). The gauge rod was adjusted, old spikes pulled, and new spikes driven in to have the gauge and cross level in good order. The switch was tested thoroughly and Jason operated the M4 for museum visitors during the process. Fine work everyone! A quick response to a new issue that had arisen. Since we had many tools out of the tool room for this work, a reorganization and clean up of the tool room was started before breaking for lunch.

 

Doug (SFHM Director) spent Saturday replacing floor in the Planer Mill and removing broken windows in the Saw Mill.

Saturday - Afternoon
Mike, Glen and Wimbley discussed the rebuilding of the Claiborne & Polk M-8 (Fairmont A-5) motor car. Glen and Wimbley have volunteered to take on much of the restoration of this car at Glen's shop and hope to have the car restored and running early next year.

Everett and Jason worked on video recording for videos on RR&G 106, the Superintendents house, the Chief Lumber Salesman's house, the Station Agent's house and the CCC museum for more videos in our Long Leaf Historical Series.

Sunday
General Engine House reorganization and cleanup. We have been devoting time to proper organization, purposeful placement of tools and items, and clean up of our high-use areas and these efforts are producing great results. The Tool Room was fully cleaned out and reorganized and it looks wonderful! Tools are hung up, accessible, and easy to distinguish. Two shovels were repaired with new handles, bolts and nuts sorted into buckets, piping and plumbing fixtures sorted into buckets, old and junk metal brought to the scrap bin, garbage properly disposed, a new light bulb inserted into the light fixtures, good rakes located, block and tackle hung up for use, and crane tools located for future use on the freshly relocated crane car.

Using the tractor, we relocated several locomotive parts and McGiffert cable to good long-term storage areas out of the way. Light fixtures and small horsepower motors were relocated to the sawmill new powerhouse for long-term storage. Using chains and the tractor, the air pump for engine 202 was relocated to the shop cart immediately behind 202. Cleanup continues along the wall next to engine house track #1 for increased space and track use. We also had time to dump out all the engine house garbage cans into the dumpster before wrapping up at midday.

Jason and Mike worked on the Bridge Crane for a bit while Everett and Tucker were working in the Tool Room. They discovered that the beam of the crane cranks up and down by hand with a ratchet mechanism, and does not run off of the engine / hydraulic pump. This mechanism will require the locating of or fabrication of a hand crank. After Jason and Tucker left, Everett and Mike played with the crane some more, and we discovered that the lifting cable mechanism may also be hand cranked through the gear box. Thus we can use the crane as soon as it is cleaned up and lubricated properly and we obtain a crank and the proper hooks. We will hope to find a crank and hooks before our next work session.

 

 

-Tucker Baker
  RR&G Road Master

 

 

Friday

 

 

 

Saturday

New whistle on 106!

 

Repairing the switch at Mainlne Jct (Switch #8) - MP 11.96

 

 

 

Mike uses a torch to heat up the switch bar so it can adjusted a bit.

 

 

Ages-old traditions and working methods are still alive on the RR&G.

 

Jason made a couple of runs with the M4 for paying customers.

 

Waiting at the Depot for passengers to board.

 

Sunday

Lifting the air pump from #202 (Two-Ought-Two)

 

Mike gingerly moved it to the back of the Machine Shop. The rear wheels of the tractor were just barely touching the ground.

 

"Easy does it..."

 

"That'll do."

 

 

 

The clean-up Tool Rooms.