Work Session

August 24, 2024

 

To join the fun, contact the railroad at: Work-Session @ RedRiverAndGulf.net (no spaces)

 

Volunteers
1. Jacques D.
2. Bryson R.
3. Mike B.
4. Mike M.
5. Everett L.
6. Angela A.
7. Andrew A.
8. Carson S.
9. Wimbley V.
10. Glen A.
11. Nick P.
12. Clint L. Jr.
13. Michael P.
14. Leo P.
15. Joseph S.
16. Gavin R.
17. Dewayne S.
18. Kira S.
19. Ayden S.
20. Kevin S.
21. Tucker B.
22. David Ham.

Accomplishments
1. M2 radiator replaced and M2 returned to service
2. Speedometers partially installed in M2 and M22
3. Deck boards installed on heavy duty MOW car
4. Three ties replaced at Main Line Junction switch and switch gauged to alignment
5. Switch repairs at Switch #9 / engine house track 1
6. General grounds maintenance of weed eating and mowing around McGiffert, engine house, and storage track
7. Old display logs removed from sawmill log intake table with forklift

Thank you to all of our volunteers who came out and contributed to a very successful weekend!

Before The Weekend
Everett located a new radiator for M2 since the leak in the old one couldn’t be sealed. Everett located a new Ford tractor radiator, and it was an exact modern match of the old radiator. Mike M drilled out the mount hole on both sides of the radiator so it would fit the existing mounts. The old radiator had been modified in the same manner. Everett procured the needed hose clamps, bolts, nuts, and washers for the radiator replacement project.

Friday
Jacques and Bryson spent time on M22 checking electrical connections and sizing up where a speedometer could be mounted in the locomotive cab. They spoke with Glen and reviewed potential ideas for a mount. Glen then fabricated small metal mounts for both M22 and M2 at his shop.

During the course of the afternoon, and Jacques showing Bryson around the museum, they found a 5 X 9 bearing. We’ll clean it up at the next session. The bearings are very useful as they can be inserted to the various railcars around the museum to facilitate movement. Many of the cars have been missing bearings for many years and having a complete set for a car that can be “swapped around” is quite helpful.

After the board meeting, Mike M, Mike B, Glen, Tucker, and David Hamilton discussed various options for recovery of the caboose frames near Sandersville after Tucker discussed options with a towing and recovery company in Alexandria. Glen, David, and Tucker went out to the caboose frames to discuss various ideas. This will continue to be a working effort through the fall and winter.

In the afternoon, Glen and Everett started installing the oak deck boards on the heavy-duty MOW car. They reviewed the plan, spaced out and staged the boards, and using c-clamps, drills, and a saw, started at one end, working to the other.

Clint, Wimbley, Jacques, Bryson, and Tucker started prep work for the M2 radiator replacement. Everett lent a torch to heat the front lower angle bar that was bent. Apparently this bar, just above the track, had been bent many years ago, as the old radiator mounts were curved to fit on this bent angle bar. After heating, Tucker and Jacques used a large Stiltson wrench Glen brought to bend the bar back into alignment. Wimbley straightened the lower radiator mounts and painted them and the fan shroud black. Might as well apply paint when we can! The crew, with Everett and Glen’s direction, then used a series of boards and a c-clamp to straighten the front frame, panels, and engine cover struts in the cab. A good clean out of the cab was also completed, including removal of many resident spiders.


Saturday
On Saturday morning, all the volunteers first gathered for coffee at the lodge kitchen. A group had rented the planer mill for a railroad-themed baby shower and requested the M4 be staged at the planer mill. The group would also be riding M4 once the shower was complete. Tucker, Kevin, and Ayden moved M4 down to the planer mill and then met the volunteer crew at the Commissary.

The whole volunteer crew gathered for the annual railroad rules clinic in the WWII room in the Commissary. Everett led a review of the Red River and Gulf Timetable and Rule Book and then the written test was administered. With the written test complete, the hands-on equipment training and certification will follow in the fall. Anyone interested in becoming a railroad equipment operator is welcome to contact the museum as additional rules training can be arranged in the future.

After assigning tasks and projects for the day, the volunteers split into crews and headed out on the museum grounds. Crew #1 of Clint, Wimbley, Nick, and Carson, with direction from Everett and Glen, installed the new radiator in M2, connected the radiator hose lines, filled the radiator with coolant, and installed the speedometer with the mount Glen made. The electrical connections will be completed at the next session.

Crew #2 of Glen, Gavin, and Dewayne worked on finishing the heavy-duty MOW car. Dewayne torch cut protrusions and obstructions for installation of the board decking. He also finished the tow bar “hitches” on each end in the afternoon. Gavin assisted as Glen led the deck installation. By the late afternoon, the car was decked and looking good.

Crew #3 of Kevin, Andrew, and Tucker clearing vegetation with weed eaters around McGiffert #1229, Main Line Junction Switch, and part of the storage track. This was to clear a good work area for tie replacement and gauging on the Main Line Junction switch later that afternoon.

Everett made several supply runs throughout the day. First getting a new toilet seat for the lodge, which he later installed on Saturday, then more bolts for the M2 radiator replacement. Leo brought sports drinks and support for the volunteers.

Joseph operated the all terrain forklift, bringing over replacement ties to the Main Line Junction switch work area. He then began removing old logs from the log intake table at the sawmill. The logs were old and falling apart, so they were hauled to a tree debris pile. The staff requested their removal so they could clean up the log intake table and control the vegetation in that area.

At midday, Tucker served as M4 motorman with Angela as conductor for the baby shower group’s ride around the loop. The ride went smoothly and the M4 interior felt comfortable with a more reflective roof now in service.

After lunch, the crews continued their work. Kira and Angela provided new volunteer orientation to Tabitha, a new volunteer looking to join the group. New volunteers are always welcome and encouraged to meet the crew at the museum on a volunteer weekend.

Joseph jumped on the museum zero turn mower and mowed around the engine house, machine shop, engine house lead tracks, around the storage track, and around McGiffert #1229 for most of the afternoon.

As the M2 radiator replacement crew continued, Tucker, Jacques, Bryson, Ayden, Kevin, and Andrew began replacing ties at the Main Line Junction switch. With the switch being on a slope of the old log pond, the crew was able to pull out three rotten ties and replace them with three stout, sturdy ties.Once the radiator replacement crew finished, and the track crew reviewed the plan at the Main Line Junction switch, all volunteers took a rest break at the lodge from the afternoon sun and heat.

After a rest and hydration break in the shade, the volunteers returned to the main line junction switch to gauge the switch. An electric cord was run from the machine shop to power a drill for pre-drilling spike holes. Everett used various bits, with assistance from Gavin and others, to drill through the rail base to securely bolt the rail in place. This was done in spots at the switch points as the switch rails prevented spiking the stock rail. Joseph, Jacques, Bryson, Kevin, Andrew, Gavin, Michael, Tucker, Everett, and Leo finished the gauging in the early evening. Work was started on realigning the washer spacing on the switch points, for a switch point “fine tuning,” which will continue at the next session.

It was a long and productive Saturday. All the volunteers lent a hand to pick up the tools from the day’s work.


Sunday
The volunteers once again split into various crews to finish up final tasks and to clean up, as per usual Sunday goals.

Everett led a crew of Gavin, Kevin, Andrew, and Ayden stabilizing switch #9 for engine house track #1. The switch tie is in fair to poor condition. The installation of several 2x6 wooden blocks helped ensure throwing the switch didn’t cause everything to go out of gauge.

Dewayne finished up the final welding tasks on the newly-decked MOW car with assistance from Angela. The car is finished and ready for service.

Everett and Dewayne also took photos and conducted a survey for David Hamilton as to the needed welding repairs on the McGiffert #1229 restoration.

Continuing the effort from the prior day, Joseph operated the all-terrain forklift with Tucker as a groundman and chainman to remove the old logs placed on the sawmill log intake table. They had all the logs removed within an hour. Joseph then used the forklift to pick up and bring the old ties removed from the Main Line Junction switch to the landscape timbers pile on the sawmill pad. Ties not good enough for the track, but still in one stout piece, are recycled as landscape timbers used to contain erosion.

As Tucker used the museum tractor to empty garbage cans at the lodge and in the engine house, the crew of Everett, Andrew, Ayden, Kevin, Angela, Kira, and Gavin begin the final pick up and clean up in the engine house. They also started the work to bring M2 from behind the M4 (over the pit for radiator replacement work), but M4 wouldn’t start. The starter was spinning, but not engaging the flywheel. Joseph came up to take a look and the crew rolled M4 over the pit for a closer look. After removing the starter, it was found that one of the screws on the bendix spring was missing. It had apparently come off during the train from the day before. Tucker didn’t turn off M4 after the baby shower folks had rode the day before, and ran M4 back to the engine house once that train was done. This fortunately placed M4 back in the engine house for this unexpected maintenance work. After checking the old starter for a replacement screw, the thread pitch on the two starters was found to be different, meaning a new screw would need to be picked up in Alexandria. Tucker brought the starter up to the workbench in the finished lumber shed so Gerald on the museum staff could locate a new screw for it.

After some final pick up and clean up tasks at the engine house and lodge, the volunteers hit the road for home. It was a safe and successful weekend. Thank you to everyone who came out and volunteered. Our next session is September 20 where we will be prepping for the 4th Annual Long Leaf Fall Festival and Steam Up in October.


-Tucker "Who Dat" Baker
  RR&G
Chief Engineer