Work Session

October 5, 2024

 

To join the fun, contact the railroad at: Work-Session @ RedRiverAndGulf.net (no spaces)

 

Volunteers
Glen A.
Wimbley V.
Everett L.
Angela A.
Andrew S.
Joe S.sd
Dewayne S.
Jason R.
Clint L. Jr.
Nick P.
MIke P.
Ben S.

Saturday and Sunday were beautiful days at Long Leaf. The volunteers took on multiple tasks in preparation for the fall festival in two weeks.

Glen worked in the morning and repaired the door on the groom's room at the bunkhouse, as well as replacing hose fittings on the two hoses in the engine house. We now have 150' of serviceable water hose for our use.

Jason and Andrew used the tractor to move debris from next to the entrance road to the burn pile.

The crew brought the M-4 up to the Engine House in preparation for running a weed and branch control train later with the M-2. When the M-4 passed the Engine House, Glen noted that it did not sound right and had Wimbley get underneath when it was over the pit. Wimbley quickly discovered that the exhaust pipe had parted at the exhaust manifold. Not a good thing.

Dewayne and Angela, assisted by Andrew, immediately went to work to repair the break. With Dewayne and his welding skills, a new, heavier pipe was welded in place and the repair is stronger than the original. It took 4 hours but by 3:00 they were done and the M-4 was again serviceable.

Joe grabbed the tractor and the finish mower and went to work on mowing and Jason started weed eating around the Engine House. Joe had started mowing on Friday evening, and mowed all day Saturday as well.

Everett had purchased piping and a valve to plumb up for a whistle connection from the air tanks in the Engine House. Wimbley, Mike, Clint and Ben worked with him to build the connection and work on the whistle from the 106 that Wimbley had located on the grounds. The piping was constructed so that the up standing pipe can be laid down and raised to allow for whistles to be changed out, or removed for safety. When Dewayne finished the M-4 he built a brace for the stand pipe to finish the job and for the first time since 1954 a steam locomotive whistle echoed over Long Leaf.

Wimbley, Clint, Ben, Andrew and Mike went to work on the loop running a brush clearing train but were cut short by the necessity of running the M-4 for crew training and an upcoming wedding.

Crew for the wedding trips was Angela as conductor and Everett as motorman. Two trips were run for the wedding party.

After running the wedding trips, crew training on the M-4 continued as we continued to qualify more operators. The addition of the speedometer makes the running of the car much easier and an operations order on the running of the car is following soon. At the end of the day, we qualified 4 more operators, bringing the total of certified operators to 14 with 2 more currently training. (list enclosed). During the training, the M-4 started experiencing air system failures. It was decided to look into that on Sunday.

After the wedding while running crew training we offered rides to the wedding party and hauled two full loads of people who then wanted tours. Angela and others gave tours to over 30 people where interested enough to promise to return to ride the train and take tours.

Saturday turned out to be a most productive 11 hour day for the volunteers!

Sunday's crew was Joe, Angela, Andrew and Everett. Joe was the most active, but Andrew and Angela did some weed clearing of the railroad by the car knockers shed, while Joe started mowing, and then decided to clean out the track leading to the #400. Once that track was again cleared, out, Everett and Joe made an estimate of what it would take to repair the track, and rebuild the switch leading to it. Doing this has been a back burner idea for several years, and now the museum has the ability to actually do it.

Everett and Angela repaired several of the spike mauls and other tools.

Joe was also called to troubleshoot the electrical problem that caused the compressor to not function. It took him less than 30 seconds to diagnose the problem as a broken fuse, which was repaired with JB Weld and the car is now fully functional. All that remains to be done is to replace the red light cover over the right rear marker light.

 

-Everett Lueck
  RR&G Superintendent