Work Session

December 14, 2024

 

To join the fun, contact the railroad at: Work-Session @ RedRiverAndGulf.net (no spaces)

 

Volunteers
1. Cody A.
2. Casey A.
3. Nick P.
4. Clint L. Jr
5. Everett L.
6. Mike M.
7. Glen A.
8. Joseph S.
9. Wimbley V.
10. Michael P.
11. Ayden S.
12. Kira S.
13. Tabitha D.
14. Abby D.
15. Tucker B.
16. Angela A.
17. Andrew A.

Accomplishments
1. Machine shop west wall beams replaced and wall secured
2. Forward-direction sanders installed on M4
3. Track cross level on main loop hill fixed
4. Additional guard rail installed at main line junction switch
5. Continued progress freeing up and lubricating locomotive 400
6. 5 ties installed on track leading to locomotive 400
7. Continued clean up and organization in the finished lumber shed


Thank you to all the volunteers that came and closed out 2024 with continued progress at the museum this weekend. Your time and talent is greatly appreciated. A big thank you for the Akins for their fabrication and installation of forward sanders on M4!

May all the volunteers enjoy a merry Christmas and we’ll all join together again in the upcoming new year.


Before the Weekend
For many weeks before December 14, the Akin brothers had fabricated two new sanding boxes at their home shop based on a sanding box from M4. They did the whole nine yards, fabrication, painting, testing, and ultimately, successful installation on M4. This session was the long-anticipated installation of sanders on M4.

Friday
Friday morning, Glen came and worked with John (staff) installing a new door at the Long Leaf Post Office. He then went up to the engine house to take photos of M8’s engine. After a compression test in mid-December by Glen and Mike M., it was determined that the rings and likely several valves needed replacement. Glen found a source for the Waukesha Engine parts for a rebuild. In the afternoon, Glen helped Mike B on one of the Heisler trucks.

After the executive committee meeting, Tucker and Doug reviewed the upcoming projects as part of the greater sawmill restoration, maintenance, and improvement push. There’s several smaller “projects within projects” at the sawmill and several of these we’ll tackle in 2025.

Friday afternoon, Wimbley, Michael, and Tucker used picks and shovels to clear the flangeways and switch frog on the track behind locomotive 400. This allowed for inspection of the ties (if any remain) on this track. As expected, ties will need to be inserted to facilitate 400’s move.

Friday evening Wimbley, Michael, and Tucker continued clean up and organization of the finished lumber shed, focusing on the tractor and lawn mower shed area. Several bucket-loads of garbage were taken to the dumpster, good lumber was organized for use the next day leveling track, scrap metal was collected and placed behind the sawmill green chain, and the area was given a good organizing. This is an effort that will continue as time allows.

Saturday
The volunteers met for the briefing at the lodge kitchen and then split into groups to work on a beautiful Louisiana Saturday morning.

Joseph inspected the all-terrain forklift after its fits at the last session. After clearing some debris in the fuel line, the forklift ran normally. The debris was after the fuel filter, so it may be the fuel line degrading. Joseph connected a battery charger to the forklift and then on Sunday, he successfully started and ran the forklift a few times to ensure everything was in working order.

After the forklift, Joseph led the effort on locomotive 400 for the day. He brought used motor oil, diesel, acetone, and automatic transmission fluid for the job. The ATF and acetone was used as a rust-penetrant to free up several joints and connections. The oil was used for lubrication in various spots. Assisting throughout the day on 400 was Angela, Nick, Michael, Everett, and others. Joseph brought an air line, Mike M lent an airline, and the shop air line was all connected together to run an airline out to 400 to clean out ports, holes, threads, etc.

Up at the engine house, Cody and Casey worked from “can til can’t” installing the forward-direction sanders on M4. Two seats were temporarily removed from M4 so the holes for the sandbox filler necks and carriage bolts could be cut in the floor. Everett and Joseph assisted in procurement of bi-directional air sanding valve and pressure regulators for the airline. Cody and Casey completed the installation, including sand line down to the wheels/rail, connection to the sanding valve, and installation of air line and regulators.

Next door at the machine shop, a third crew of Glen and Mike M worked on the machine shop west wall. Several lateral beams had been replaced in the wall several years ago, however, they were replaced with smaller beams, resulting in several unfavorable multi-joint beam meets. Throughout the rest of the machine shop walls, you could see the original, proper beam lengths and how they maintained a very strong wall structure. This situation on the west wall partially led to the wall bend during a major high wind event in the area earlier in May. Mike measured and then ordered two quality 20-foot beams in advance and had them on hand for the session. Mike even positioned some beam supports and braces with additional lumber until the repair could be completed. Mike and Glen completed the lower section of the west wall, replacing the damaged sections of 2x8s with the new beam. The upper beam will require temporary scaffolding to reach, to be completed at a future date. Raising the beam to the top side of the window will be challenging! The goal is to change the framework of that window so that it can be opened as intended and strengthen the wall. With the wall secured in place, another upcoming project will be installing landscape timbers/ties to function as an erosion control wall / dirt retaining wall on this side of the machine shop.

A fourth crew of Wimbley, Michael, Tabitha, Ayden, Abby, Andrew, Tucker, Everett, Clint, and Kira went out on the main loop with M2 and the herbicide car loaded with old lumber pieces to level the hill track in a few spots. Much material is recycled at Long Leaf, and lumber found and /or leftover from other projects is reused. A piece of lumber rotten on one end or one spot is still good - cut out the bad and put it to use leveling track. Using track jacks to raise the track, blocks were cut from lumber, knocked under ties, and the ties tamped to hold level. The next good rain will then fill in dirt ballast completely under the ties. The crew raised and fixed about 5 areas on the hill track, making a good improvement for the morning.

After lunch, Everett, Joseph, and Tucker inspected the spot where Joseph derailed on M2 a few weeks prior. After checking cross level and gauge, it was decided to install another rail to function as a longer guard rail on the uphill side (machine shop side). As Cody, Casey, and Everett made a hardware supply run into Alexandria, Tucker, Andrew, Clint, Michael, Wimbley, Tabitha, Ayden, and Abby tackled the guard rail installation. Tucker and Andrew used the tractor to bring over a bent 60 pound rail from the pad, one that would work as a guard rail but would not do for standard track rail. Running electrical cords from the machine shop, holes were drilled, the rail held in place with lining bars, and spikes driven in to hold the newest guard rail in place. M2 tested operation over the guard rail and all was found to be in good order.

After the hardware run, Cody and Casey continued their work on the M4 sand boxes. Nick, Everett, Angela, and others continued to work in and around locomotive 400. With the tractor and the track tools on hand, Michael, Tabitha, Wimbley, Abby, Ayden, Clint, Tucker, and Andrew installed 5 ties on the track leading to 400 at Switch #5, lower Clyde siding. This involved digging out slots for the ties, removal of old tie debris, sliding in ties, gauging the track, drilling holes, and using the electric hammer to drive in the spikes. Being right next to the engine house, extension cords were run to power the electric tools.

In the evening, as Cody and Casey continued working on the M4, Joseph and Tucker worked on installing hinges for the two M4 seats that would sit above the sand box filler necks. Leftover spare lumber was measured and cut by Joseph, and after sorting through a screw bucket to find a matching set, the first hinged seat was put together.

Everett, Angela, and Andrew, noticing some lights bulbs out in the engine house, grabbed a ladder and the light bulb extension pole to install new light bulbs. The spring holding the light bulb grabbing end on the pole broke on the 2nd bulb change, so Everett planned on getting a new one and a few more light bulbs that evening.

Sunday
On Sunday, the volunteers finished up some efforts and continued others. Everett and Angela changed out the burnt-out light bulbs in the engine house with the new light bulb extension pole Everett got the night before.

Joseph continued lubricating 400 and working toward dropping the eccentric crank connections.

Andrew and Tucker completed the hinges on the second M4 seat. Once Cody and Casey were done with the sanders, the two seats were reinstalled in the M4. The hinge action was found to be satisfactory to access the sanders for refilling in the future.

Once the sanders were complete, Cody, Casey, Joseph, and Tucker went to fire up M4 and to take it for a test spin. After initially starting up fine, the engine puttered out. Fuel level was checked, and more fuel was put in. Still the issue of starting and struggling then dying out persisted. After troubleshooting the engine, the issue was found to be with the carburetor. After testing with the idle screws, pinching the fuel line, and other tests, the float was not working properly, allowing in fuel inadvertently. The matter would be followed up on with the staff and potentially more troubleshooting at the next session.

Wrapping up the session was the lodge clean up. Everett went through upstairs making sure all was in order. Joseph and Tucker emptied garbage cans, swept the kitchen, and mopped the bathrooms, kitchen, and even the front porch. That way the lodge starts clean for the new year in 2025.


After the Weekend
Gerald (staff) checked the M4 carburetor, and sure enough, there was an issue with the float. Debris had gotten in, causing the float to not work. He cleared it and reinstalled the now-working-again carburetor. Mike M has already plumbed a metal fuel line with a new fuel pump, but hasn’t switched over the line yet. He’ll do so soon to replace the rubber fuel line, which is potentially degrading and causing its debris to get into the carburetor.

Glen moved the M-8 to his shop on December 23rd. The engine is scheduled to be disassembled, and the cylinders will be measured for rings and valves before ordering any parts. Glen hope’s to perform this without removing the engine block from the car for the rebuild. Removing the front wheels and axle should provide ample clearance to remove the oil pan to access the connecting rods. A speedometer will also be installed before its return. He’s unsure of the rebuild time, but I hope to have it back as soon as possible. After researching the M-8 engine, Glen reports he found it to be a FC(Parson) engine. The serial # FC86K was built between 1937-1946. The 3-1/4" bore is rated at 35HP@ 2400 RPM; Most were produced for the Fairmont A-5 railcar.

Trivia- The F= Full compression lubrication
The C= Comet Conversion, Military High Output
The K= Larger Bore, Kerosene fueled engine after WWII



-Tucker "Who Dat" Baker
  RR&G
Chief Engineer